Lost turbo boost

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Viewing 15 posts - 1 through 15 (of 21 total)
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  • #69685

    Tubsy250
    Participant

    UK - England

    Posts: 206

    Driving  my car home tonight driving quite hard ,changed into fifth gear and service light came on and lost boost ,pulled over    turned car off and then back on no service light and full boost again car only done 3000 miles.Drove another 10 miles using full throttle as many times as I could and all is well? could it be an electrical gicth

    #69688

    red-leader
    Participant

    UK - England

    Posts: 2372

    Another thought, it could be a sensor connection. Had a similar issue on my Cosworth which was a bad connection into the ECU.

    #69695

    jasoni
    Participant

    UK - England

    Posts: 346

    I have had exactly the same thing, has only ever done it once. A member on here read about the same issue a guy had on another forum, that the symptoms experienced could be down to a poorly performing wastegate solenoid which Ford confirmed and changed under warranty. If it happens again take it in to the dealer.

    #69697

    Tubsy250
    Participant

    UK - England

    Posts: 206

    That sounds about right it’s was boosting but only about .25 bar like the wastegate Was opening and dumping the boost

    #69714

    o1turbo30v
    Participant

    USA

    Posts: 160

    It’s called an overboost fault that caused the car to go into limp mode, basically the turbo was making more pressure than the ecu wanted, the ecu couldn’t control it fast enough so it went into limp mode, reduced power and boost, surprised you got that on stock programming

    #69718

    Tubsy250
    Participant

    UK - England

    Posts: 206

    The car running mountune fpm375 tune

    #69720

    jasoni
    Participant

    UK - England

    Posts: 346

    As mine is tubsy

    #69724

    rs-le
    Participant

    UK - England

    Posts: 372

    Hi all

    This week I had fpm done, warmed up from dealer, 1st full beans squirt in 2nd & 3rd , display showed engine service now! “Wtf”, when I arrived at my destination 3 miles later, turned car off , then on , message gone, not done it since? Not due a service for a few months yet either and mileage is low. Oil level ok , topped up once ,1/4 litre after 1st 1500 miles a couple of months ago, Water level ok.

    um , will go back to dealers if it happens again…

    #69742

    gary1234
    Participant

    UK - England

    Posts: 900

    to be honest I have had that on mine I was told to lock the car then re open it twice and it would solve it

    never done it since it was 2 days after fpm installed ,

    #69748

    Tubsy250
    Participant

    UK - England

    Posts: 206

    Hi spoke to fred at mountune today, and he said if you hit the Rev limiter it can cause the issue which mine did,so nothing to worry about  must learn to change gear quicker done to many miles  in dsg car .

    #69750

    rs-le
    Participant

    UK - England

    Posts: 372

    Cheers tubsy250 I was on the limit lol, nice bit of info, memo to self change gear quicker lol ?

    #99376

    Eddiewin87
    Participant

    Australia

    Posts: 31

    @Tubsy250

    I’ve just had this exact same problem. Thank the Flying Spaghetti Monster for this club. I can find anything that could go wrong with the RS here.



    Aussie V8 rivalry is dead.

    Holden V8 Traitor.

    xForce 3″ catback varex exhaust

    Mountune Cold Air Intake

    Forge Recirculation Valve

    Dreamscience Ultima 2

    Magnetic Grey

    Gel spoiler inserts

    #108474

    stteb
    Participant

    UK - England

    Posts: 173

    I lost boooost the other day ..

    took the under tray off , a clamp came loose on my hard pipe from turbo to intercooler , which I upgraded about 5 months a go .

    #140180

    Cedric Vanraemdonck
    Participant

    Belgium

    Posts: 1

    Hey guys, i need your advice.

    my car threw a check engine light yesterday.
    went to the shop, put it in obd and got some turbo fault codes.
    It makes insufficient power/ boost but there seams to be no leakage.
    Its a 2016 ford focus rs, mountune intake, mountune recirculation valve and muffler delete. No further tuning or so …. anyone got advice or had this problem before ?

    #151815

    Hotdog9087
    Participant

    UK - England

    Posts: 3

    Hello, new to the site.
    rather than starting a new thread, can I add to this?
    I have a 2016 RS running race de-cat, forge uprated recirculating valve and dreamscience v3 re-map.
    was driving along today (not raking it) and there was a huge loss of power. There are no warning lights on, no noise or smoke but the turbo gauge doesn’t move on acceleration and the car is slow to pick up.
    Any ideas!  T.i.a.

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